Even now there is a lot of uncertainty around this crash, maintenance - or lack thereof - or even wrong maintenance could still be a factor. But given the location of the part asking for a 'visual inspection' is a pretty strange move, the part is all but inaccessible when it is in its normal position and even with an endoscope it would be pretty hard to determine whether or not the part had weakened. That's just not going to show up visually until it is way too late unless the part has been especially prepared to announce the presence of hairline cracks.
You'd have to disassemble a good chunk of the wing to gain access to the part based on the pictures I've seen of how it all holds together when assembled.
The same happened with MCAS, the pro-Boeing argument was that if those were American pilots it would have been fine.
Boeing knew of the flaw, and sent a letter to airlines about it. In 2011.
There's a lot of gray going on here.
Doesn't seem like gray to me. It seems a company who has a history of cutting corners and ignoring or downplaying safety problems did exactly that in this case too which resulted in the deaths of many people. UPS made an error here as well in trusting Boeing when they said it wasn't a safety issue and they should have installed the revised bearing assembly out of an abundance of caution, but I don't know much they would have known back in 2011 about the changes at Boeing that prioritized profit over safety following the merger with McDonnell Douglas
Because my naive conclusion after looking at the part in question is exactly the same "would not result in a safety of flight condition." if the bearing cracked at the point in question it is going nowhere, the bearing is still captive in its housing. hell it looks like it could have been designed as two pieces and it would work the same. the large bolt is what is holding the engine on.
The best I can come up with is that a split bearing causes increased wear on the mounting bracket and nobody noticed for a long time.
Anyhow, here is the ntsb update in question https://www.ntsb.gov/investigations/Documents/DCA26MA024%20I...
So if that bearing went that's not quite a smoking gun yet but it would definitely be a step closer to a root cause.
To reduce negative outcomes, we use risk management: assessing the likely lifetime cost of the flaw, and taking cost-effective measures to reduce the risk to an acceptable level. As a familiar example, redundant mass storage drives are much more cost-effective than high-reliability mass storage drives.
I am not an expert, however. Can metal fatigue be detected with such infrequent inspection?
[1]: https://en.wikipedia.org/wiki/Aircraft_maintenance_checks#AB...
On things like D check, the aircraft is essentially completely taken apart and inspected at that level typically taking 50,000 man hours and 6 month-1 year of time.
The article mentions the cost and that Boeing underestimates it. When you divide the cost by the number of hours, it seems very reasonable. Parts and materials being included. I’m surprised any job that extensive isn’t even more expensive.
It was also insanely expensive to operate: $300k/hour in 1990 dollars, and there aren’t reliable numbers on development costs with all of the black budgets.
I know satellites and drones have replaced the sr71 but it would be cool if someone would build a plane as capable again.
I also expect that they were much less complex than an aircraft that provides a comfortable, pressurized cabin; the high level of safety mentioned above; freight capacity; etc.
Also, despite Boeing's recent problems, I would guess that commerical passenger planes are far more safe than they were decades ago when the SR-71 was developed. Accidents were much more common despite many fewer flights, iirc.
Obviously they could have designed something that could expand and contract if they thought it was worth it.
Also, this was done because airframe skin temps exceeded 400F during flight due to the high speeds.